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               The GOOD, the BAD the UGLY of the 9.2 KEEL BOLTS

Just finished the 9.2 keel bolt project. The bolts are actually .752" rod, threaded 2" on each end. ( 3/4" by 10 per inch, but not a normal SAE thread) They extend down into side pockets on each side of the keel except the front and aft ones that are on centerline, the keel is too thin to put in pockets. The the photo to the left, shows the 3 keel pockets that are visible and the erroded / corroded bolt in the front has broken. This allowed the keel to pull away from the hull. I was fortunate that this is not SilverSwan.  I found all of my bolts almost as good as new. That is the beauty of a fresh water boat.
9.2 keel exposed pockets
 

I extracted 3  bolts and examined them and also had a metallurgist inspect them. No pitting, no crevice corrosion, no galvanic corrosion. They looked like they were installed last month.  Not bad for 24 yr. old bolts, but a fresh water boat for its entire life.   Cast iron and mild steel have almost the same galvanic potential, stainless is a little further up the scale, 430 is much closer than 304.
The pockets were originally packed with can foam and then faired with an epoxy mixture. Water ran out of the pockets when I ground down to them. Easy to find  the pockets, they can  have a little surface distortion,  or with a strong magnet.  I used a strong refrigerator magnet to check the distorted area to confirm that they were the pockets.



keelpockets I used an angle grinder to get to the pockets and then pried out the foam from around the bolt and nut. I tried to just open the faring to minimize the amout of work. I only had 2 weeks to seal the bolts and fair the work areas at the keel pockets. I used a dremmel tool to clean the inside of the pockets down to the cast iron. I tried a  filled epoxy blend ( the dark red-brown in the photo on the right) for ahesion to the bare cast iron  prior to the whole job. I took a lot of abuse and the epoxy itself failed, not the bond to the cast iron.

I ran a dremel tool with a wire brush attachment over the threads to clean them up. I brushed McLube ( Krytox dry film lube) on all threaded sections and also coated the threads of the nuts. Rotational friction kills clamp load when tightening. MoS2 dryfilm lube would also work well. The bolts if mild steel, worst case, would have a proof load capability of around 55,000psi. or 24,700lbf. It sounds like overkill until you consider the bending moment applied to the bolts when the boat heals. Even with a worst case moment applied the bolts are only subjected to around 7,000lbs in shear and tension. The amount of bolts is more for load distribition to the cross ribs and the thickened hull section.

The original packing,sealant was cotton balls with a white sealant that over the years had turned to dust. I had 3 definate leakers and the possibly existed of a couple weepers. The inside of the bilge around the bolt locations were wire brushed and wiped clean with acetone. In a couple spots the bilge was not flat with respect to the bolt, so I utilized thickened epoxy and a plastic form to put the bilge on an even keel.  The brown filled epoxy is evident under the right bolt next to the cross stringer.( below) This was also the bolt that I threaded with a SAE die to clean up the threads. The new nuts would then work.
keel bolts
Sealant ( 4200 fast cure) was injected into the bolt to hull gap, packed in best  possible with a bead built up around it, a little bead on the back side of the load washer and carefully placed over the threads to keep them clean. I used a stack of 3 where possible to keep the sealant out of the threaded area. I tried to use new 3/4"x10 nuts , but the nuts jammed and would not assemble. The right-most stud was modified by running a SAE 3/4x10 die over it on both ends. It did make a little pile of shavings and did an excellent job of cleaning up the threads that I buggered up with a cold chisel removing the froozen nuts. I carefully cleaned the threads in the old nuts and coated them with the McLube, dry lube.

 All bolts were snugged down well and a final load applied 24hrs later to seat the keel to hull. A small bead of sealant oozed out around the bottom of the stack of washers. I estimate that I applied 120 to 150 ftlbs of torque to tighten the bolts. This should result in approxamately 10,000 to 14,000 lbs of clamp load for each bolt. That should keep the keel snug to the hull.                                                                                                                                                                                                                             
 
epoxy coated I decided to protect the nut and threads from direct contact with the epoxy by placing a little sheet of plastic overthem and then the pockets were then  packed with highly filled epoxy.  The local boating store no longer carried the WEST SYSTEM  in favor of the MAS EPOXY brand. I did not have any experience with it for cure times, so I chose the med cure rate. As usual, I really wanted a little faster cure time due to the colder weather.
This filled epoxy will be very easy to dremel out or use a chisel if I need to get back in. I wanted to be able to tighten the nuts in the bilge if necessary without having to manually secure the nuts in the pockets with a wrench. ( the problem that started this whole project) The keel area was faired with several layers of filled epoxy, and then the usual sealant  followed by VC17.  I used the original VC17, clear resin with copper powder mixed in. The old bottom paint looked like an old penny, the new bottom paint just like it was fresh from the mint.
I'll wait a week and splash her the next Sat, AM just in time for our CLSC Long distance Wyss Race. I single handed and arrived 2 minutes after the start.

keel faired


Total time for this quick project was 4 man days. We do not have the ability to drop the keel and completely re-bed. If in salt water, I believe that this would be far better.
A quick note on stainless bolts, it is subject to crevice corrosion. This occurs when the stainless is bathed in salt water without flow. It stagnates and the water is depleted of O2. The result is that the stainless cannot oxidize to protect itself, pitting begins and develops a + and - charge in the pit that is self feeding thanks to the NA+ and CL- ions.  If you decide to use stainless bolts, consider the 400 series instead of the 300 series to reduce the galvanic cell potential. ( contact folks that do this for a living) You may have to re-bed the keel to hull joint to prevent water weepage as well as packing the nut pockets in the keel. I don't know how to encapsulate the bolts with a removable compound should service ever be necessary.

prop martec

The biggest problem experienced:
I ran a die over the threads of one of the bolts. It was a ¾”x10, and removed a little material. It did a great job of cleaning up the threads. Normal ¾”x10 nuts would now fit, before they acted too small. I made me believe that a special tap and die were used for the keel bolts not the standard 6G, 6H thread classification commercially available today. I used a cold chisel to bust off a couple of the frozen nuts and new ones did not fit. If you know the reason why let me know.

The prop on SilverSwan is a 14Dx12P RH Martec Eliptical. I snapped a pic for reference. She will cruise at 6.5 knots running at 2900RPM which is well within the limits of the 2GM20 Yanmar engine. I burn a tank a year, about 12 gallons. I add cetane and bio treatment in the fuel  for the winterization. I will still go out if the weather is over 50F. I just have a few extra gallons of antifreeze on board to treat the engine when we return to the dock.

Keel bolt repairs on some boats is difficult due to the bolts being "J" bolts molded into the lead. In this case the old bolts are left in place and new ones are added, by the process of "sistering". They just drill, tap, epoxy new studs in place doubling up. Through the Islander 36 site I found Don Huseman (310-547-4604) who travels around the USA doing just this. He quoted in the ball park of $2,000 to travel with tools and do 8 new bolts. Considering the alternatives of being in east Tennessee, no marine service centers, it looked like a good alternative if necessary. (HusemanD@netscape.net)
In the case that the old ones leak, it is common practice to encapsulate them with epoxy.  When I found a loose bolt that did not tighten I feared the worst and considered this method.  I believe that the pockets are an OK method and easy to service if you have a full service marina with a travel hoist. It then would be possible to remove and fully re-bed the hull to keel joint.

Link to MAS EPOXY http://www.masepoxies.com/


Eric
SilverSwan #19
Cal 9.2